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Efficiency analysis of a high-specific impulse hall thruster

Publication ,  Conference
Hofer, RR; Gallimore, AD
Published in: 40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit
December 1, 2004

Performance and plasma measurements of the high-specific impulse NASA-173Mv2 Hall thruster were analyzed using a phenomenological performance model that accounts for a partially-ionized plasma containing multiply-charged ions. Between discharge voltages of 300-900 V, the results showed that although the net decrease of efficiency due to multiply-charged ions was only 1.5-3.0%, the effects of multiply-charged ions on the ion and electron currents could not be neglected. Between 300-900 V, the increase of the discharge current was attributed to the increasing fraction of multiply-charged ions, while the maximum deviation of the electron current from its average value was only +5/-14%. These findings revealed how efficient operation at high-specific impulse was enabled through the regulation of the electron current with the applied magnetic field. Between 300-900 V, the voltage utilization ranged from 89-97%, the mass utilization from 86-90%, and the current utilization from 77-81%. Therefore, the anode efficiency was largely determined by the current utilization. The electron Hall parameter was nearly constant with voltage, decreasing from an average of 210 at 300 V to an average of 160 between 400-900 V. These results confirmed our claim that efficient operation can be achieved only over a limited range of Hall parameters. © 2004 by the American institute of Aeronautics and Astronautics, Inc.

Duke Scholars

Published In

40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit

Publication Date

December 1, 2004
 

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Hofer, R. R., & Gallimore, A. D. (2004). Efficiency analysis of a high-specific impulse hall thruster. In 40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit.
Hofer, R. R., and A. D. Gallimore. “Efficiency analysis of a high-specific impulse hall thruster.” In 40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit, 2004.
Hofer RR, Gallimore AD. Efficiency analysis of a high-specific impulse hall thruster. In: 40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit. 2004.
Hofer, R. R., and A. D. Gallimore. “Efficiency analysis of a high-specific impulse hall thruster.” 40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit, 2004.
Hofer RR, Gallimore AD. Efficiency analysis of a high-specific impulse hall thruster. 40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit. 2004.

Published In

40th AIAA ASME SAE ASEE Joint Propulsion Conference and Exhibit

Publication Date

December 1, 2004